This last Wednesday we were coming back from Southern UT (more on that when I get a minute to post some pics) and we stopped to get some fuel. Coming out of the FBO, I saw a Balanca flown by a local guy come in for a touch and go. After a bounce he landed and then was off for another lap around the pattern. By the time we reachedour aircraft at the self-serve pumps, he was about to come over the numbers. That is when my flying buddy said something about his gear not being done. Sure enough. There was no time to warn him so I ran to where I had a good view of his touch down. Shortly I heard the first, and then second sound of the prop striking the asfault, following by the engine going to full throttle. Talk about a low energy go-around. The plane wallowed for a few moments and them reluctanty start to fly in ground effect. Well beyond the end of the runway, it was still very low. It banked to the left and then banked steeply to the right. At that point we thought it was the beginning of a stall and waited to watch it go down. We really thought we were going to watch someone die. But, the plane leveled heading south and slowly started to gain some altitude. It was hard to hear whether the engine was running smoothly or not.
Seeing that he was gaining some altitude, I jumped on the radio to see if he was going to make the field. When I turned on the radio, I caught the last of his transmission. He said that he was returning to runway 26 for an emergency landing. I asked if he was going to make the field and he said he would, after he explained that he had made a "blunder". I told him that we were on the ground and saw the whole thing. We told him we would wait to depart until he got back on the ground. He landed uneventfully and was able to taxi it in to the tie-down area. We met him at the plane. Understandably, he was shaken, but glad to be alive. All three blades were curled over and both inboard edges of the flaps had dragged the runway. He told us that he had just gotten it back from having an annual done on it and this was the first chance he had to fly it. The engine had around 100 hours on it. I'm just glad it turned out the way it did. It could have been a lot worse. I think we left there with a look similar to this.

